Went to a Ford dealer and talk to the service department. They never heard of such a thing. The one guy went about and talked to all his mechanics for about 15 minutes and came back with the same answer. There was no service bulletin issued for this motor to have a shorter connecting rod installed. He told me if it ran fine before I took it apart minus the head gasket leak then if I correctly reinstall all the parts back the way it was then it should run fine. He said if I was worried about it that much that I should pull the motor and replace the piston and rod in question. I cant pull the motor since I have no way of doing so. I will just put back everything and cross my fingers that it will run like it did for the past 2 years minus the head gasket leak. He did say that gas mileage will suffer some because of the lower compression on that cylinder. He also told me to put a hotter plug in that cylinder. There was no shaking stumbling anything when I drove the van, it ran fine. There is plenty of power before I tore down the motor, and it passed emissions here in my state. Gas mileage was 18 city 20 on highway. He did mention that due to the piston having a stamped number on top that it was more than likely replace at some point. That's the answer I got from our local ford dealership.